Hodakaguy M38 Misc Thread

Start your project thread here for advice and for others to follow along with your project. This is a long term thread.

Moderator: wesk

Post Reply
HodakaguyTom
Member
Posts: 79
Joined: Wed Apr 24, 2024 6:00 pm
Location: Eastern WA State

Post by HodakaguyTom »

wesk wrote:Using a hammer on alternating sides of the bearing shell can and often does result in uneccessary wear on the opening. Much better to drive the bearing race squarely with a round adapter or even a piece of pipe or large socket.
Agreed. This fit is a fairly "loose" fit and was easy to work into place by carefully going back and forth. I do usually use a pipe for this application and agree it's the better meathod. Thanks Wes.

Hodakaguy
HodakaguyTom
Member
Posts: 79
Joined: Wed Apr 24, 2024 6:00 pm
Location: Eastern WA State

Post by HodakaguyTom »

Back at it....

Time to seat the front bearing race and mount the front bearing housing.

Adding some engine assembly lube to the pilot bearing so it won't start dry.

Image


Just in case I ran into any unforeseen complications I decided to assemble the bearing housing onto the case with a dry gasket to set the depth of the outer bearing race then pop the housing back off to apply sealant to the gasket once the bearing race is set into position. The depth of the bearing race is set by the protruding lip on the front bearing retainer. You want to tap the retainer with a mallet and slowly tighten the bolts of the retainer back and forth to work the housing all the way down against the case, don't just try tightening the bolts to pull the bearing retainer down as you run the risk of breaking an ear off the retainer casting.

Image

Image

Image


Bearing race seated and front bearing retainer removed once again. Be really careful pulling the shift rails through the seals since they are already installed.

Image


Prepping the gasket with Aviation Permatex. I've used this sealant for years with great success, it can be messy but it just plain works.

Image

Image

Image


Slowly working the cover back on for the last time, taking care to make sure the lip seals don't get cut or folded during assembly.

Image

Image


Permatex #2 on the bolt threads. I'm using copper washers under the bolt heads for extra sealing protection, with Permatex #2 under the copper washer as well.

Image

Image


Torquing the bolts to 30 ft/lbs

Image

Image


I decided to leave the interlock pill out of the shift rails, this will allow us to run low range while in 2wd....great for creeping along slowly in parades ect without having to ride the clutch.

Image


Dropping in the shift rail indent balls and springs. I added some gear oil to the spring/ball before installing the cap but I did have a suggestion to add some grease to these parts so I may pull them back apart and add some grease before installing them back in the jeep.

Image

Image

Image

Image

Image

Image

Image


With the front bearing housing complete it's time to turn my attention to the rear output shaft

Image


To start I checked out the original bolts I had removed from the rear bearing housing and the threads were in poor cond. I ran a die over them to clean up the threads but they had a loose fit when threaded into the case so it's time for new bolts. I had some grade 8 bolts so I drilled some safety wire holes in the bolt heads and now had nice snug fitting bolts for assembly.

Image

Image

Image


When I took the transfer case apart I found .182" worth of shims and an end play of .0365".....waaaaay out of spec! Since I'm starting with new bearings I wanted to get an approximate idea of where to start on the shim pack. I tapped the bearing race into place (was a little on the loose side so I will add some Loctite 640 to the race upon final assembly) and got it to about .010" end play, I then used feeler gauges to measure the gap where the shims go with the bearing cap held lightly in position against the bearing race. This was a start...then I would adjust from there.

Image

Image


Each time the shim pack was adjusted I would install the new shims, torque up the rear bearing housing to 30 ft/lbs, tap on the front and rear housings several times with a mallet to seat the bearings then measure the end play with a dial indicator. If the play was to large then it was off with the assembly, adjust the shim pack and repeat the process. These steps were repeated several times.

Image

Image

Image


Factory specs for end play is .004" - .008". Sal from Vintage Jeeper prefers a tighter setup and Novak recommends tighter clearances as well...002" - .006". Playing with a combination of my new and old shims I was able to get the end play set at .0027". Perfect.

Image

Image


Happy with my end play I started prepping everything for final installation. I'll be using copper washers under the bolt heads for added sealing benefits. Ignore the star washer on the short bolt, it gets a copper washer as well.

Image


Pay attention to the three sizes of bolts and where they go into the bearing housing. One bolt is 1/4" shorter than the others, this is necessary to clear the shift fork, if a long bolt is installed in this position it will limit the throw of the shift fork.

Image


Adding Permatex #2 to the bearing housing to prevent any oil from seeping out between the bearing cap and emergency brake backing plate, if any oil ever gets by the threads. I also mounted the emergency brake arm before I added the backing plate with the sealant on it.

Image

Image


Since I didn't feel like the race was a tight enough fit in the case I carefully worked the race back out of the case and applied Loctite 640, this will retain the bearing in the case firmly once installed. If your using this be very careful not to get any on the inner race.

Image


Copper Spray a Gasket applied to the flange surfaces and both sides of the shims. NOTE: This is the point you want to install your speedometer drive gear onto the rear output shaft.....before you install the rear bearing cap. Notice mine isn't installed here? More to come on that below lol.

Image

Image

Image


Applying Permatex #2 to the bolt threads and under the copper washers.

Image


Back on the case and torquing to 30 ft/lbs for the final time.

Image

Image


Verifying final end play clearance after everything is assembled.

Image

Image

Image


Added safety wire to the bolt heads.

Image

Image


And that is that.....or is it? I hit the bed for the night, woke up at 4am this morning...went to roll over and within 30 seconds of waking up thought..."Dang! I didn't install the speedometer drive gear!". By 4:10am I was back out in the shop taking the assembly back apart to install the gear. I had thought about this set several times during assembly, but never took the time to take the parts out of my parts bin and place them up on the table with the other parts so I wouldn't forget them. Totally my fault on this one and lesson learned.

Image


The Copper Spray a Gasket had set up very well! Brake clean on a rag did a great job of cleaning up the shims and mating surfaces once again.

Image


Installing the speedo drive bits into the rear bearing retainer.

Image

Image

Image

Image


Ahhh....the step I missed that let me do all of this again lol.

Image

Image

Image

Image


Assembled once again, bearing retainer torqued to specs, new copper washers installed on the bolts, fresh Permatex #2 on the threads and under the copper washers and end play clearance verified once again. Right on the money.

Image

Image

Image


More to come.....

Hodakgauy
User avatar
4x4M38
Member
Posts: 3487
Joined: Thu May 29, 2014 6:00 pm
Location: Texas Hill Country

Post by 4x4M38 »

No way this is intended as criticism. This article is gold.

I have read several places that to clean threads you should use a thread chaser and not a die. The chaser has more clearance than a die, and won’t necessarily cut new metal like a die can. The die could remove enough metal to cause a looser fit like you experienced.

Just my two cents.

Keep it coming please!!
HodakaguyTom
Member
Posts: 79
Joined: Wed Apr 24, 2024 6:00 pm
Location: Eastern WA State

Post by HodakaguyTom »

4x4M38 wrote:No way this is intended as criticism. This article is gold.

I have read several places that to clean threads you should use a thread chaser and not a die. The chaser has more clearance than a die, and won’t necessarily cut new metal like a die can. The die could remove enough metal to cause a looser fit like you experienced.

Just my two cents.

Keep it coming please!!
Thanks Mate. Your right about the thread chaser vs tap, I had used a tap when a thread chaser would have been a better option in this situation. I have a full set of chasers on hand now. That said the new bolts are a nice snug fit in the case, the threads on the old bolts were definatly past their prime. Glad your enjoying the thread and thanks for chiming in...sharing info and ideas is what makes these forums great.

Hodakaguy
RonD2
Member
Posts: 2065
Joined: Wed Oct 01, 2014 6:00 pm
Location: South Carolina, Dorchester County

Post by RonD2 »

Not stock, but I'm using magnetic drain plugs on the T90 and D18 (also on the L134 oil pan).

While there's some debate about it being "correct", I painted my drain plugs red --- although paragraph 67.d. (2) on page 50 of the January 1956 TM9-8012 says just the refill plugs get that "bling". :D

And while really not "correct", in the same spirit I use these on the 20+ something grease zerk fittings so I can find them easier and keep crud out of them at the same time: https://locknlube.com/products/copy-of- ... 7761618004

Awesome photography!
Ron D.
1951 M38 Unknown Serial Number
1951 M100 Dunbar Kapple 01169903 dod 5-51

“The only good sports car that America ever made was the Jeep."
--- Enzo Ferrari

HodakaguyTom
Member
Posts: 79
Joined: Wed Apr 24, 2024 6:00 pm
Location: Eastern WA State

Post by HodakaguyTom »

RonD2 wrote:Not stock, but I'm using magnetic drain plugs on the T90 and D18 (also on the L134 oil pan).

While there's some debate about it being "correct", I painted my drain plugs red --- although paragraph 67.d. (2) on page 50 of the January 1956 TM9-8012 says just the refill plugs get that "bling". :D

And while really not "correct", in the same spirit I use these on the 20+ something grease zerk fittings so I can find them easier and keep crud out of them at the same time: https://locknlube.com/products/copy-of- ... 7761618004

Awesome photography!
Thanks Mate, Iike the idea of a magnetic drain plug...may do the same thing. :-)

Hodakaguy
HodakaguyTom
Member
Posts: 79
Joined: Wed Apr 24, 2024 6:00 pm
Location: Eastern WA State

Post by HodakaguyTom »

Well...waiting on a few parts to finish up the transfer case so let's check out the clutch and install a fresh pilot bushing.

Bell housing removed.

Image


Pressure plate and clutch disk removed

Image


Pilot bushing visually looks ok...but I'm here and have a new one on hand so its time to yank the old one and install a new unit.


Using a blind puller to remove the old pilot bushing.

Image

Image


And installing the new bushing.

Image

Image

Image

Image

Image

Image


The clutch assembly and flywheel have little time on them and the old unit was working nice and smooth....butttttt....it's all apart so I think I will install a fresh clutch and pressure plate while it's all opened up. New Parts on order from Sal at Vintage Jeeper....back to waiting.


What else can I do today....ah yes, magnetic drain plugs.

Magnetic drain plugs are available for the transmission & transfer case but they have the civilian square heads on the plugs. I'd like to keep the correct round headed drain plugs for the M38 so figured I would just make my own. Magnetic drain plugs are a great addition, if you can trap any little metal bits on the drain plug and keep them from circulating through the bearings and bushings that's a huge win.

New drain plug and 1/4" rare earth magnets. Rare earth magnets are very resistant to losing their magnetism when stuck to metal over long periods of time... Perfect for this application.

Image

Image


Drilling a 1/4" hole in the bottom of the plug to accept the magnet.

Image

Image

Image


Test fitting the magnet in the hole. Nice snug fit and the magnet holds itself there nice and tight.

Image


Cleaning the plug and magnet of any oil and dirt.

Image


Using Loctite 660 quick steel to secure the magnet in the plug. Magnet was twisted 1/4 turn while inserting. Once seated the excess was wiped off and part was left to cure.

Image

Image

Image

Image

Image


Self etching primer & paint applied. Ready for service.

Image

Image


Hodakaguy
User avatar
4x4M38
Member
Posts: 3487
Joined: Thu May 29, 2014 6:00 pm
Location: Texas Hill Country

Post by 4x4M38 »

And I was wondering where to buy magnetic plugs…
RonD2
Member
Posts: 2065
Joined: Wed Oct 01, 2014 6:00 pm
Location: South Carolina, Dorchester County

Post by RonD2 »

I cheated and bought mine here: https://www.thecj2apage.com/forums/tran ... 46896.html

Notice these magnets are mounted flush inside the plug body.

While Tom does superb work, I'd offer that I heard these rare earth magnets can be fragile --- if you accidentally drop the plug and it lands on the magnet it could break or chip?

Just a thought.
Last edited by RonD2 on Mon Jan 06, 2025 11:13 am, edited 1 time in total.
Ron D.
1951 M38 Unknown Serial Number
1951 M100 Dunbar Kapple 01169903 dod 5-51

“The only good sports car that America ever made was the Jeep."
--- Enzo Ferrari

HodakaguyTom
Member
Posts: 79
Joined: Wed Apr 24, 2024 6:00 pm
Location: Eastern WA State

Post by HodakaguyTom »

RonD2 wrote:I cheated and bought mine here: https://www.thecj2apage.com/forums/tran ... 46896.html
Nice, thanks for the link! Those look great, For that price I would have just purchased those instead of messing with it if I had known they were availabe.

Hodakaguy.
RonD2
Member
Posts: 2065
Joined: Wed Oct 01, 2014 6:00 pm
Location: South Carolina, Dorchester County

Post by RonD2 »

RonD2 wrote:I cheated and bought mine here: https://www.thecj2apage.com/forums/tran ... 46896.html

Notice these magnets are mounted flush inside the plug body.

While Tom does superb work, I'd offer that I heard these rare earth magnets can be fragile --- if you accidentally drop the plug and it lands on the magnet it could break or chip?

Just a thought.
Sorry! I should have included the link up front.
Not sure they're still available.
Ron D.
1951 M38 Unknown Serial Number
1951 M100 Dunbar Kapple 01169903 dod 5-51

“The only good sports car that America ever made was the Jeep."
--- Enzo Ferrari

User avatar
4x4M38
Member
Posts: 3487
Joined: Thu May 29, 2014 6:00 pm
Location: Texas Hill Country

Post by 4x4M38 »

You could Chuck them up and cut them off in the lathe.

Heck, make a few more and sell them. You have the magnets…
RonD2
Member
Posts: 2065
Joined: Wed Oct 01, 2014 6:00 pm
Location: South Carolina, Dorchester County

Post by RonD2 »

4x4M38 wrote:You could Chuck them up and cut them off in the lathe.
Pretty sure that won't work.

See this: https://www.kjmagnetics.com/blog/how-ne ... s-are-made

"Neodymium magnets are formed by powder metallurgical methods. Their mechanical properties more closely resemble a ceramic, rather than a metal.

They are not easily machined, and we don't recommend trying to machine them.

Neodymium magnets are very hard and brittle. Despite the metallic appearance of their nickel plating, they are not strong as steel. If subjected to sharp impacts, such as allowing them to slam into one another, they can easily crack or break. Care and proper handling are important.

We don't recommend press-fitting neodymium magnets. Magnets are often glued into a pocket that is slightly larger than the magnet, rather than press-fitting."
Ron D.
1951 M38 Unknown Serial Number
1951 M100 Dunbar Kapple 01169903 dod 5-51

“The only good sports car that America ever made was the Jeep."
--- Enzo Ferrari

HodakaguyTom
Member
Posts: 79
Joined: Wed Apr 24, 2024 6:00 pm
Location: Eastern WA State

Post by HodakaguyTom »

Waiting on a couple transfer case parts to arrive so we can finish that project up. Time to get a couple smaller items out of the way while we wait.

Re-installing the clutch. The clutch we removed was in great cond with very little time on it, we will re-install this unit.

Image


New Chromoly flywheel bolts from Vintage Jeeper.

Image


The old input shaft I removed from the transmission makes a great clutch alignment tool.

Image


Flywheel ready for clutch install.

Image


Going back together. Input shaft in place to align the clutch disk.

Image


Manual calls for 12-17 ft/lbs of torque on the bolts. I torqued them to 16 ft/lbs.

Image


And ready for service.

Image


Next up....swap out the fuel filter. When we purchased our Jeep it had been sitting for years with old fuel in the tank. The fuel had turned to a white powder which is not only hard to clean out of the tank but is great at clogging fuel lines, filters and carburetors. We are currently in the process of cleaning out the fuel tank so it can be re-lined, while that is taking place it's time to get the fuel filter assembly cleaned up and ready for service once again.

OEM filter vs the new Stainless Steel filter assy.

Image

Image

Image


The original filter has deformed allowing a gap to open up at the bottom mounting plate, allowing crud and powder to bypass the filter and make it's way into the fuel lines etc.

Image

Image

Image


The new Stainless Steel filter from Peter Debella's is available as a stand alone filter or you can purchase it as a complete assembly with a new stand pipe, end plates and bolt. I had ordered a complete new assembly, now to clean everything up and get it installed.

Image

Image

Image


Filter material is sealed into the end caps with adhesive.

Image


Ready and awaiting a clean fuel tank for re-installation.

Image


Hodakaguy
HodakaguyTom
Member
Posts: 79
Joined: Wed Apr 24, 2024 6:00 pm
Location: Eastern WA State

Post by HodakaguyTom »

Parts are in......onward!

We received our new Intermediate gear assembly from Vintage Jeeper this weekend....sweet! This unit has been modified to use tapered roller bearings instead of the needle bearings that the OEM setup uses. Tapered bearings is a better fit for this duty, it will wear better, run cooler and be quieter than the OEM setup. With the new parts in hand it's time to assemble this baby.

Here's the tapered roller bearing intermediate gear assembly as received from Vintage Jeeper.

Image

Image

Image

Image


The gear is machined to accept the tapered bearing races.

Image


The shaft is sealed via two O-rings that are opposite the tapered end. Thrust/bearing pre-load is set by tightening the castle nut and pushing the spacer into the case.

Image


Time to get this baby together. You'll notice that I removed the E-brake backing plate yet again, the shaft is inserted from this end and the backing plate was in the way. If you're building your transfer case plan ahead and install the intermediate gear before installing the brake backing plate.

Image


A little light assembly lube on the bearings.

Image


And some quality standard grease on the bushing and O-rings.

Image


Inserting the intermediate gear into the case.

Image


Carefully insert the shaft into the case. Tap the shaft into position with a rubber mallet.

Image

Image

Image


Insert the busing being careful not to pinch/cut the O-rings.

Image


Checking/setting thrust on the bearings. I set thrust at .0015", rule of thumb is .001" per inch/diameter of the shaft. Thrust can be easily reset any time by dropping the oil pan and re-adjusting the castle nut while the transfer case is installed in the Jeep.

Image


I ground a small flat spot on the bottom washer to clear the case. I ended up using two washers to get the proper height on the castle nut.

Image

Image


A fresh coat of copper spray a gasket.

Image

Image


Re-checking thrust on the output shaft. Still right on the money.

Image

Image


Installing the emergency brake assembly.

New shoes.

Image

Image

Image

Image


Rear companion flange installed along with new bolts and a fresh felt.

Image

Image


A 24" crescent wrench works great to hold the output shaft in place while torquing the rear output companion shaft and front output yoke nuts. I used the original castle nuts that came with the NOS output shaft as they are 3/4-20 thread pitch, a size that is non standard now.

Image

Image

Image


Masking the front output yoke in preparation for primer/paint.

Image


Fresh paint. The paint will darken when dry and loose it's high shine.

Image


The lock tab on the intermediate gear wasn't a great fit, time to fabricate a new one.

Image

Image

Image

Image

Image

Image

Image


Adjusting the emergency brake shoe clearance.

Image

Image

Image


Done except for the oil pan install. Waiting for the paint to dry on the bolts.

Image

Image

Image

Image

Image


More to come soon....

Hodakaguy
Post Reply