SUCKING OIL
Posted: Fri Jul 13, 2012 6:36 pm
UP THROUGH THE DIPSTICK !!!
RAN 6 MILES TO THE LOCAL BS STATION..SAT AROUND BS-ING FOR 1/2 TO 45 MINUTES IT WAS HARD TO START BY THEN FROM SITTING..
HEADING HOME STARTED MISSING SO I PULLED CHOKE OUT ABOUT 1/2 MOTHERED IT HOME , GOT IT HOME AND THERE WAS OIL IN THE SHORT X-OVER TO CARB HOSE AND THE CARB WAS FULL OF OIL..
I CLEANED IT ALL OUT ..STARTED SEARCHING AND DONE THE FOLLOWING
CLEANED UP AND REPLACED 24 VOLT PLUGS RE-GAPPED @ .30
CHECKED TIMING & DWELL SPOT ON
REPLACED POINTS CONDENSOR COIL ALL WITH NOS STUFF I HAVE HERE
CHECKED PCV VALVE --CLEANED IT OUT
CHECKED COMPRESSION 106 104 105 101
CHECKED OIL LEVEL JUST A KISS UNDER FULL MARK
CLEANED OUT AIR CLEANER NO OIL WAS BEING SUCKED THROUGH IT
NOR WAS IT IN THE LONG HOSE FROM AIR CLEANER TO X-OVER TUBE
M38 IDLES @ 32 LBS PRESSURE
IF I REMOVE THE SMALL RUBBER HOSE FROM CARB HORN TO X-OVER TUBE REV UP THE ENGINE I CAN SEE OIL PUSHING OUT INTO THE X-OVER TUBE & PUSHING OUT THE TOP OF THE OIL TUBE ..38 STILL RUNNING FINE NOT SMOKING BLUE OR WHITE
I CAN PUT MY HAND ON THE TOP OF THE OIL TUBE AND FEEL IT HAS PRESSURE PUSHING AND MY HAND IS BLACK WITH OIL..
I GIVE UP WHAT AM I MISSING OR WHAT DO YOU GUYS & GAL THINK IT COULD POSSIBLY BE ????
I HAVE BEEN TOLD IT IS VERY POSSIBLE I HAVE A BUSTED COMPRESSION RING..ALSO TOLD IT COULD BE CRACKED VALVE..???
MY SIDE-KICK IS NO LONGER WITH ME SO I AM OUT OF OPTIONS AS TO WHAT TO FIX NEXT ..HE WAS THE MASTER OF THIS STUFF AND IS NO LONGER WITH US..HONESTLY THIS IS THE FIRST TIME I HAVE EVER HAD EVER SEEN THIS HAPPEN ...
I WAS RUNNING THIS ABOUT 7-15 MILES EVERY COUPLE WEEKS AND IT RAN FINE.ALL I DID WHEN I BOUGHT THIS WAS GO THROUGH IT ,,HAD THE CARB, FUEL/VAC REBUILT FROM THEN & NOW , REDO THE GAS TANK AND REPLACE THE BATTERYS IT WAS RUNNING FINE UP UNTIL LATE THIS AFTERNOON...
ANY HELP OR IDEAS ...THANKS
RAN 6 MILES TO THE LOCAL BS STATION..SAT AROUND BS-ING FOR 1/2 TO 45 MINUTES IT WAS HARD TO START BY THEN FROM SITTING..
HEADING HOME STARTED MISSING SO I PULLED CHOKE OUT ABOUT 1/2 MOTHERED IT HOME , GOT IT HOME AND THERE WAS OIL IN THE SHORT X-OVER TO CARB HOSE AND THE CARB WAS FULL OF OIL..
I CLEANED IT ALL OUT ..STARTED SEARCHING AND DONE THE FOLLOWING
CLEANED UP AND REPLACED 24 VOLT PLUGS RE-GAPPED @ .30
CHECKED TIMING & DWELL SPOT ON
REPLACED POINTS CONDENSOR COIL ALL WITH NOS STUFF I HAVE HERE
CHECKED PCV VALVE --CLEANED IT OUT
CHECKED COMPRESSION 106 104 105 101
CHECKED OIL LEVEL JUST A KISS UNDER FULL MARK
CLEANED OUT AIR CLEANER NO OIL WAS BEING SUCKED THROUGH IT
NOR WAS IT IN THE LONG HOSE FROM AIR CLEANER TO X-OVER TUBE
M38 IDLES @ 32 LBS PRESSURE
IF I REMOVE THE SMALL RUBBER HOSE FROM CARB HORN TO X-OVER TUBE REV UP THE ENGINE I CAN SEE OIL PUSHING OUT INTO THE X-OVER TUBE & PUSHING OUT THE TOP OF THE OIL TUBE ..38 STILL RUNNING FINE NOT SMOKING BLUE OR WHITE
I CAN PUT MY HAND ON THE TOP OF THE OIL TUBE AND FEEL IT HAS PRESSURE PUSHING AND MY HAND IS BLACK WITH OIL..
I GIVE UP WHAT AM I MISSING OR WHAT DO YOU GUYS & GAL THINK IT COULD POSSIBLY BE ????
I HAVE BEEN TOLD IT IS VERY POSSIBLE I HAVE A BUSTED COMPRESSION RING..ALSO TOLD IT COULD BE CRACKED VALVE..???
MY SIDE-KICK IS NO LONGER WITH ME SO I AM OUT OF OPTIONS AS TO WHAT TO FIX NEXT ..HE WAS THE MASTER OF THIS STUFF AND IS NO LONGER WITH US..HONESTLY THIS IS THE FIRST TIME I HAVE EVER HAD EVER SEEN THIS HAPPEN ...
I WAS RUNNING THIS ABOUT 7-15 MILES EVERY COUPLE WEEKS AND IT RAN FINE.ALL I DID WHEN I BOUGHT THIS WAS GO THROUGH IT ,,HAD THE CARB, FUEL/VAC REBUILT FROM THEN & NOW , REDO THE GAS TANK AND REPLACE THE BATTERYS IT WAS RUNNING FINE UP UNTIL LATE THIS AFTERNOON...
ANY HELP OR IDEAS ...THANKS